And then it was done. But not until the project took a few unexpected twists and turns.
Last time, I was in a quandary over how to assemble the points to the fulcrum. I was convinced I needed to reinforce the assembly with pins or plates or something extra. But as I pondered the situation, I decided not to modify the points; I felt it might pose a risk of damaging them. So I elected to make the plastic fulcrum part as large as practical to create the greatest surface area possible between points and fulcrum, so as to increase the likelihood that a straight CA bond would be enough to keep things together.
Just making the plastic fulcrum piece, though, was quite an ordeal. I can't recall ever investing so much time in making a single little styrene rectangle—well over an hour spent on something that measures all of about a half inch long by 90 thousandths at the wide end, tapering to 40 thousandths at the other end.
Most of the work went into figuring out exactly how it had to be shaped. You see, it needed to hold a point rail such that each end was in precise contact with both the stock rail and the frog at the same time. Then it had to be able to rotate a degree or two and place the other point rail in precise contact at both ends. That's four precision points to hit on a moving part. That's hard work. Not to mention that one edge had to be ever so slightly curved for the diverging route point.
As for its fabrication, it was a relatively simple—if time-consuming—process of taking a few swipes with a fingernail file, measuring, test fitting, and repeating these steps countless times. And for all of that effort, the part couldn't be more uninteresting-looking:

And that was just the half of it. The following hour was spent attaching the points to the fulcrum. For this step I arranged a vaguely Rube Goldberg-ish looking contraption, with clamping tweezers clamped in a vice—plus a ruler thrown in so that the cork backing would make up for the difference in the sizes of the tweezer handles. Once I had this kluge jig set up, the real time-sucking work began as I had to measure exactly where the points needed to be positioned relative to the fulcrum.

What made it so complicated was that the bottoms of the point rails did not sit flush with the bottom of the fulcrum. This was by design—I didn't want the point rails rubbing on the base of the switch. So, it was measure, tweak, measure, tweak, repeat, repeat, and then, after a swig of wine to calm the nerves, it was time to apply the CA.

CA can surprise you. It can bond some things furiously well, often when a super-bond isn't even needed. Other times it completely fails to bond at all—even on combinations of materials that had proved successful in the past. On this occasion, when I released the point assembly from the clamps, it just fell apart, as if I'd applied water instead of CA. (This product became famous under the trade name "Krazy Glue"—and an apt name it is.)
Time for Plan B. What was Plan B? Solder the points to a metal fulcrum, and pretend it's plastic. Actually, Plan B
used to be my Plan A; I'd originally intended to make the points out of a single piece of metal to demonstrate how simply it could be manufactured. But the potential of shorting pushed me toward the more
conservative design approach of electrically isolating the point rails by using a plastic fulcrum.
No matter; the switch would work either way, and assuming there's sufficient clearance for the wheel flanges, nothing bad will happen. (If it did, I could use the old fingernail polish trick to add a layer of insulation on the sides of the points.) Since I had a plastic pattern for a new metal fulcrum, the hard work was already done, and Plan B got going quickly.
To simplify the assembly, I used .010-inch thick nickel-silver, as this was the clearance between the bottoms of the point rails and the switch base. I could simply solder the points right to the surface of the nickel-silver, then trim the nickel-silver down flush to the sides of the points.


After soldering the parts together, I determined the precise center of rotation and drilled a hole in the fulcrum, then drilled the corresponding hole in the switch base. I tapped the hole in the fulcrum for a 00-90 screw, then made a bushing from a sliver of thin-walled brass tubing.

The flea-sized bushing (above, just to the left of the screw) was crucial to the proper functioning of the points: it provided a smooth bearing surface for the hole in the plastic base—as opposed to the screw threads—and also allowed the screw to be tightened without binding the mechanism.

With the points temporarily mounted, I marked the throwbar for the pin that would move the points. This was just a small square of plastic bonded to the throwbar.

After about two hours of fine-tuning, I was at last rewarded with a nicely-snapping set of switch points. At this point I covered the nickel-silver fulcrum with the original plastic one, which I'd sanded thinner to account for the thickness of the metal under it.

But enough about building the darned thing... how does it work—
with trains? Ah, for that, you'll have to wait until the next installment. I'm a real stinker, aren't I?